logxlogx

EN
nan4
画板 1 拷贝
TECH-EXHI
Recommendations
Fluoride salt batching system and its application
2020.01.19

Summary:A PLC + weighing instrument realizes the structure, working principle, system characteristics and control method of the fluoride salt automatic batching control system.The control system adopts standardized, modular and systematic design, with flexible configuration, convenient configuration, system reliability and good on-site application effect.

Aluminum Corporation of China Qinghai Branch 85,000 tons of electrolytic aluminum technology reform project (hereinafter referred to as "8.5 project") in the fluoride salt dosage system of technological transformation, the use of PLC + weighing instrumentation (connected to the weighing module) + industrial computers, the successful automation of the fluoride salt dosage, the application of the effect of a good.

1 Control system overview

The composition of weighing control system is based on the existing dosage system, combined with the expansion of the new system process equipment configuration of the automatic control program. The newly expanded "8.5 project" fluoride salt batching system includes two sets of systems in the east and the middle, each set of systems has two alumina silos, four sets of fluoride salt fixed volume discharger, two sets of weighing and displaying instrumentation; control of the dosage system includes two sets of industrial controllers, one set of PLC control system, two on-site operation boxes and dosage scales of the control device. Among them, the industrial control machine is mainly to complete the formula management, historical data query. The core of the control system consists of a set of SIEMENSS7-300 series PLC, which mainly accomplishes.

1) supply and transportation control of raw materials.

2) material proportioning control of the formula; 3) communication and data exchange.

3) communication and data exchange, PLC and two industrial control machine composed of Ethernet, to facilitate the establishment of the future plant LAN and data transmission.

2 Working principle and design characteristics of batching control system

The dosage control of the dosage control system is carried out according to the formula ratio and control requirements inputted by the operator, and calculated by PLC according to the pre-set kilograms of fluoride salt dosage in batches. Firstly, set the high and low limits of alumina hopper, such as the high limit is set to 2500kg, the low limit is set to 500kg, and ton/aluminum needs to be matched with 20kg of alumina fluoride, then input: (2500-500)120=100 in the column of "formula number", the PLC will control the change of the actual measured value of fluoride salt according to the electronic weigher during the process of hopper discharging after the logic operation. After logic operation, the PLC controls the number of times and the interval time of the action of the cylinder of fluoride salt discharging according to the actual measurement value of the electronic scale in the process of discharging, i.e., for every 100kg of alumina, the fixed capacity cylinder with the capacity of 1kg will act for 1 time, and when the discharging speed of alumina is accelerated, the interval time between the action of the cylinder of fluoride salt discharging will be shortened accordingly to achieve the even dosing of fluorinated alumina. When the actual amount of material in the hopper reaches the low limit value, PLC sends a signal to the low material valve of the hopper and the fluoride salt discharging cylinder to stop discharging, and the dosage is completed, and then proceed to the next assembly process. In the remote terminal real-time display of the actual amount of alumina hopper and fluoride salt cylinder action times, industrial control machine in the CRT with text, dynamic graphics and digital display of the current actual dosage.

The control design of dosing and conveying must be combined with the actual working conditions of the cleanroom site.

The movement mechanism installed on the top and bottom of the hopper - cylinder, sealing, dust collecting device in the process of starting and stopping, if it is not necessary to carry out the necessary hardware and software processing, it will have a very big impact on the control accuracy of the dosage system. The structural form of the sensor and the structural form of the mounting accessories. Limit device of weighing hopper and anti-vibration method. Weighing change display device and PLC signal connection form and in the program BCD signal error code processing design.

Various types of valve structure in the design of the site should be combined with the characteristics of the working conditions to prevent leakage, blocking, not in place and so on. In order to prevent the inverter pollution of the power supply, instrumentation and other control power supply circuit should be added with a power filter to purify the power supply.

Improvements in the installation of the sensor, so that the hopper is not easy to produce relative displacement, to avoid the hopper random offset brought about by the many troubles and weighing and dosage of precision instability.

3 load cell signal acquisition

Load cell is actually a quality signal into a measurable electrical signal output device. Selection of load cell should first consider the working environment in which the sensor is located, which is related to whether the sensor can work properly as well as its safety and service life, and is related to the reliability and safety of the whole scale. The choice of load cell level must meet the following two conditions: ① Meet the requirements of the instrument input. Weighing instrument is the output signal of the sensor after amplification, AD conversion and other processing to display the weighing results, therefore, the output signal of the sensor must be greater than or equal to the size of the input signal required by the instrument, i.e., the output sensitivity of the sensor must be calculated to be greater than or equal to the input sensitivity required by the instrument. ② Meet the requirements of the entire electronic scale accuracy. Electronic scale is mainly composed of three parts of the scale, sensor, instrumentation, the choice of sensor accuracy should be slightly higher than the theoretical calculated value, because the theoretical calculated value is often subject to the limitations of the objective conditions, such as the scale strength, instrumentation performance, the scale's working environment and other factors, will directly affect the scale's accuracy requirements.

There are three types of load cells for electronic scales: series, parallel and hybrid. The parallel connection has the advantages of strong anti-interference ability and minimum number of power supply bridges (only 1). The reason why the parallel connection, but also take into account the clean room dosage site environmental conditions are poor, such as vibration, interference, dust and other factors

The installation of weighing module must pay attention to:①The lead cable of the sensor should wear iron pipe, and it should not be too close to the power line, it should be more than 50cm. ②)The cable must be four-core or six-core shielded cable. ③ in the same scale on the three sensors must be the same range, the force is also best to be consistent, also known as "pressure four corners", the output is consistent in order to achieve satisfactory results.

4 Upper computer software design

The industrial control configuration software IFIX launched by the U.S. Intellution is a powerful industrial automation software products. IFIX configuration software provides powerful functions required by industry, including real-time monitoring and supervisory control, alarms and alarm management, historical trends, statistical process control, user safety systems, system extensions, network functions and so on. It provides a visualization window for process processing, which enables the interface to provide graphical process information, including raw data, calculated data, variables, trend graphs, alarms, etc. IFIX's powerful graphical functions show the control point information of the dosage process in a clear way. IFIX open development interface can be embedded in the user's third-party language source program (such as C, VB and other languages), with good ease of use and flexibility to become the first choice of industrial control software for the "8.5 Project" expansion and reconstruction projects. The dosage control system can also be connected to the intranet through a switch, and can set the on-site control parameters in the control room; it can display the leakage of each scale so that the operator can take corresponding countermeasures; in the case of a long period of time without interrupting the dosage of the scale empty signal, the operator can determine the cause.

5 Conclusion

In the "8.5 project" fluoride salt dosage system technical reform project development process, the application of DDE technology to the powerful configuration software IFIX and rapid development tools VB combination, so that the recipe function to obtain very good results. Not only can more than 50 formulas be saved, but also the modification and updating of the formulas are convenient and flexible until the communication is transmitted to the PLC.

SRS Marriage system
The mixing system is an on-line measurement dynamic measurement system which integrates the functions of transportation, measurement, batching and quantification. The weighed material automatically descends according to the preset formula, and the actual blanking error is automatically corrected at the next blanking. After weighing, set early mixing according to the discharging time to avoid uneven mixing in the mixing bin. 混配系统适用于定型、不定型耐火材料以及其它行业的配料自动化控制,适合于物料的连续计量和生产过程中的配料作业。使用本系统可有效提高配料精度,提升产品质量,大大降低工人劳动强度,提高工作效率,改善工作环境。基本做到配料车间微尘化、配料工作无人化,降低企业生产成本和管理强度,提升企业生产装备技术水平和产品的科技含量。 投料系统可自动根据配方要求控制移动配料称量车自动在256(可以更多)个料仓下完成多种料的计量配料,到每个排料口自动卸料,控制室内采用工控计算机及PLC系统(DCS),移动配料称量车上安装称重专用控制仪表(简称下位机)和电子秤,上、下位机之间通过通讯线连接。上位机操作使用汉字菜单和图形显示,屏幕动态显示移动配料称量车位置,动态显示配料重量,自动监测系统是否正常,整个配料线状态在工控计算机屏幕上可一目了然,系统还可记录打印各次配料结果,打印日报表、月报表,电脑最多存储1000个配方。 配料控制系统根据客户生产工艺要求采用PLC编程控制 使用组态监控系统作为人机操作控制界面,完成各种配方输入和动作命令的控制。通过人机组态监控系统和PLC程序控制对加载到称重配料车的物料进行称重、流量的控制,从而实现准确计量和配料,提高效率。 技术参数: ①微机自动控制整个生产过程;用户操作员可制定、修改、编辑生产配方; ②液晶显示器可监控设备的自动工作运行状态; ③微机可以存储多种生产配方; ④电子料斗秤采用双速加料控制方式,保证加料既快又准确; ⑤自动停车对位精度:±10mm;单料斗最大称重量:300~1500kg; ⑥内轨距、车体高度、卸料口形式见图纸(可按用户工艺修改); ⑦ 环境温度:称量车工作现场 -20℃~+50℃,微机控制室 0℃~+30℃; ⑧ 工作方式:微机自动操作,控制室半自动操作。 ⑨ 称量电子料斗秤的进料口安装了能自动升降的密封装置以及除尘系统,可以有效地解决加料和卸料过程中的粉尘飞扬问题,使生产现场环境清洁有序; ⑩ 电源功率:380V±10%,50Hz,11~37Kw,控制系统工作电源:AC 220V±10% ,50Hz,0.5Kw;
Weighing and mixing machine in powder dosage system application program
The whole automatic batching system consists of industrial control machine, PLC, industrial weighing instrument, frequency converter, vibration motor, mixer, sensor, conveyor belt and other parts.
Powder Dosing System Design
The automatic dosage system consists of an industrial grade control computer, programmable controllers, and electrical control boxes, and is designed to meet the needs of a maximum number of silos and platform scales for mixing, weighing, and mixing control.
Screw dosage system technology application
Screw automatic dosage system is the ideal equipment for continuous dosage and measurement of bulk materials, which can set high, middle and low feeding, and then control the feeding speed of screw feeder, so as to achieve the purpose of accurate dosage. According to the actual process of batching process, it reflects the operation status of feeding, batching, feeding and related equipment in the form of dynamic screen.
Application Design of Weighing Mixer
Weighing and mixing machine through PLC to control the frequency converter, so that the speed motor drives the metering screw according to the set speed running down the material. The whole weighing and dosing system can be divided into small material weighing, large material weighing and micro material weighing. It adopts the way of uniform speed feeding, and the way of decreasing speed feeding is adopted in the low speed stage.
×